Engine Transmission Pull

With a cheap harbor freight hoist the 20r engine and R43 transmission have been pulled. The block crank and head will be taken to a local shop to get bored honed and rebuilt. Cylinders didn’t look to bad for 80k miles. Since the Chinook had a blown head gasket, my guess is that it overheated since the thermostat was shot & the head bolts didn’t appear to be torqued properly.

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Pertronix Ignition

Worked on outlining the changes i need to make to the ignition. This includes the replacement of points to Pertronix electronic ignition. Got a replacement Accell coil, and confirmed that its resistance/voltage allow for the removal of the white resistor. It supports higher voltage, like the flamethrower coils. Otherwise the voltage is too low for […]

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Engine Bay Cleanup

Rust Cleanup begins, cleaning and de-greasing.

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The Intake is leaking!

So it turns out the metal coolant plate under the stock intake isn’t a very good design. it’s a dissimilar metal from The Aluminum Intake and it looks like it’s Stamped Out of sheet metal and coated in zinc. I cleaned mine since it was super corroded and thought I could reuse it but apparently […]

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